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Thread: Trailer Wheel Hub Repair

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  1. #1
    Supporting Member hemmjo's Avatar
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    Trailer Wheel Hub Repair

    I have a small home made utility trailer with a damaged wheel hub.
    Link Question on Wheel Hub Repair

    A bearing went bad and damaged one of the hubs. (My fault, lack of maintenance)
    Good hub with the bad one. The lack of paint and amount of rust tell me this has been
    failing for quite a while

    Click image for larger version. 

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    To begin the repair it I bored the damaged area, where the seal fits.

    Click image for larger version. 

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    Then needed to made a bushing to fit into the new bore.
    I have had a broken rod from a hydraulic cylinder around the
    shop for over 40 years. Too nice a piece of steel to sell for scrap.

    Click image for larger version. 

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    The seal end already had a hole so I took a slice off that end.

    Click image for larger version. 

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    Face first side

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    I have recently begun using carbide more often. It was a necessity for this steel.
    When facing, the relation of cutting speed to surface finish became very evident.

    Notice the matte finish and the cool chip in this frame from a video

    Click image for larger version. 

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    As surface speed increased as diameter increased,
    the chips turned blue and surface finish like a mirror.

    Click image for larger version. 

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    Holding the part inside the bore to turn the OD to 0.004 under the
    hub bore and and begin to cut the thickness.

    Click image for larger version. 

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    Then holding on the OD, began boring the ID.

    Click image for larger version. 

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    As boring progressed I realized that jaw pressure might
    distort the bushing.

    Click image for larger version. 

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    The finished wall thickness will only be about 0.050”.
    Each cut made me more concerned about distortion. I stopped
    when the wall thickness got close to 0.150”

    Click image for larger version. 

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    Ready to install

    Click image for larger version. 

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    Test Fit

    Click image for larger version. 

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    I had a couple of initial ideas for installing the bushing.
    After considering a press fit, I decided to use adhesive.
    JB weld and Red Loctite came to mind. When looking for
    the Red LocTite, I found a bottle of LocTite 680 Bearing
    Retainer in my tool box. The bottle was dated 2019, shelf-life
    Is supposed to be 2 years. I needed to know it is was still good.

    I made a test by drilling the threads out of a nut and using the
    680 to “glue” it to a smooth piece of steel.

    Click image for larger version. 

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    Click image for larger version. 

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    After curing a couple of days I broke them apart, holding the shaft in the
    Vise and using a toque wrench. Beginning at 25 pound-foot, increasing
    by 5 pounds until it failed. It held100 pound foot. 105 pound foot broke the bond.

    Click image for larger version. 

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    I have no data, but that seems like a good enough bond to hold the bushing.
    I used LocTite 680 bearing retainer to install the bushing in the hub.
    Then let it cure for a couple of days.

    Click image for larger version. 

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    I took light boring cuts of 0.005 (.0025 DOC) to avoid
    heating the LocTite too much. It became apparent during the
    first pass that the chuck had distorted the bushing.
    The skipping cuts could be easily heard, 3 times,
    equally around the bore. Before making the second pass I put
    layout die in the bore which clearly showed the 3 jaw locations.

    Click image for larger version. 

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    The 3rd pass almost eliminated the distortion.

    Click image for larger version. 

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    The bushed hub with its un-damaged brother. You can see,
    the transition between new and original but I cannot feel it

    Click image for larger version. 

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    Click image for larger version. 

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    Now waiting for Speedi-Sleeves for the spindles

  2. The Following 2 Users Say Thank You to hemmjo For This Useful Post:

    emu roo (Nov 18, 2025), nova_robotics (Nov 18, 2025)

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